Aero Energy LM1600 LPT Installation, Engine Installation, and Package Alignment April 18th through 27th, 2014 For Princeton University ESN 751-533 Under GE Oracle Project 7255815 Customer Representative: Eric Wachtman GE Field Service Representative: Matt Wilson All technical recommendations and information contained in this report are based on GE manuals that have been developed and approved for use with GE engines and parts that have been operated and maintained in accordance with GE technical documentation and recommendations. GE has no technical knowledge of, nor obligation for, non GE-approved parts and repairs. Accordingly, this report is not intended to apply to non GE-approved parts and repairs, nor to any parts that may be directly or indirectly affected by non GE-approved parts and repairs. LM6-212 - V.4 Aero Energy LM1600 Overview: The purpose of this report is to document the maintenance with 751-533 that took place during the April 2014 outage. During this time the GG was removed, the LPT was replaced, and the engine was re-aligned after a separate generator gearbox inspection. Outage Data: Engine Data: ESN Model 751-533 LM1600 SAC Maintenance Data: WP, SB, SL, PB, PL Performed WP 208 00 Engine Fired Hours Engine Fired starts Revision/manual reference WP 500 00 LPT Module Removal and Replacement Gas Generator Handling N/A Package Hours 126,846.76 N/A Package Fired Starts 736 Date completed 18 April 2014 Comments 18 April 2014 Components Found Not Serviceable: Detail Findings: PAC Number (if available): Notifications (SM/CPM/PM/ENGR/SL or FSRM): Leaking CDP Flexible Hose. N/A CPM Follow Up Action Items Engineering: None Follow Up Action Items SM/CPM/PM: Order and ship to site flexible braided stainless steel hose for CDP System. Hose Information: 1 1/4” Stainless Steel Hose x 16” long MFG P/N 2796 32696-1 Reference Princeton F&ID 92904-B-2529 Revision 5 Item number on F&ID is M1305 Report completed by Matt Wilson LM1600 2 Aero Energy LM1600 LPT Removal and Installation General maintenance information for the work done on both units: - During reinstallation the original match-marks were used from the November disassembly. - The machined alignment pin was checked for proper installation to make sure the LPT case was installed in the correct orientation to the gas generator. Seating check measurements were taken on both GG’s and LPT’s prior to disassembly. The information on both units is provided in the following pages. LPT match marks aligned LPT nut installed and teeth engaged LPT Module removed from engine Alignment pin on LPT case Report completed by Matt Wilson LM1600 3 Aero Energy LM1600 LPT Module Seating Information: Measurement A was taken on the LP shaft prior to LPT installation. This was added to dimension X, the thickness of the seating flange on the low-pressure turbine to ensure a proper seat. The actual thickness is within the calculated thickness tolerance of +/0.001”. The flange bolts on the LPT case were lubricated and torqued to 155 inch-lbs. 751-533 Replacement LPT Dim A 0.279" Check without LPT Installed (Dim. X) 0.2745" Check after LPT was replaced 0.554" Calculated Drop 0.554" LPT Identification Markings The table below shows all identification marks found on the LPT modules that were swapped. Customer LPT Module Assembly 6042T05G06 Serial Number GGM9E8W9 Assembly Unknown Serial Number Unknown Miscellaneous 60497T69P03 GATHDMLP Example of identification marks found on LPT Rotors Report completed by Matt Wilson LM1600 4 Aero Energy LM1600 Engine Installation Turbine View Right side Turbine View Left side Inlet inspected and free of debris Mesh Screen Replaced Floor checked and cleaned prior to start up No leaks identified during crank/ leak checks Report completed by Matt Wilson LM1600 5 Aero Energy LM1600 Engine Installation IGV’s and VSV’s inspected. No loose hardware, worn lever arms, guide pins or outer bushings identified. Lease covered prior to can loading Open lines and connections covered for shipment Aft view of GG Aft view of GG Report completed by Matt Wilson LM1600 6 Aero Energy LM1600 Package Alignment: TARGET (+/- 0.010” Rim; +/- 0.005” Face) RIM FACE 0 0 0 0 0 0 0 0 AS FOUND RIM FACE 0 0 -5 +30 -5 +25 +5 -1 AFTER ALIGNMENT RIM FACE 0 0 -8 +8 -1 0 +2 +1 AXIAL DISTANCE TARGET (+/- 0.010) AFTER ALIGNMENT 42.000” 41.990” 42.000” 42.000” 42.013” 42.006” 42.000” 41.990” Average: 42.000” Average: 41.999” Report completed by Matt Wilson LM1600 7 Aero Energy LM1600 Start up details Friday April 25, 2014 Replaced mesh FOD and completed final inlet inspection. LOTO removed for start up and testing on gas. First start was fail to fire due to ignitor circuit breaker not being turned on. Two more fail to fires occurred with gas valve operations appearing normal and fuel gas pressure sufficient for start up. An investigation into the ignitor condition and ignition system was completed with no faults identified. The system was restored and light off on gas was successful by the end of the shift. During this run to full speed no load, it was identified that PT speed probe #1 was not reading, and channel A on the PT vibration accelerometer was also not reading. The unit was shut down and LOTO performed to investigate. The speed probe and accelerometer connections were found to be secure. Due to the high tempurature of the exhaust and back end of the PT no futher work was conducted. Saturday April 26, 2014 Replaced PT vibe accelerometer from customer stores for troubleshooting. PT speed probe connections were removed cleaned and re-seated. LOTO removed for liquid fuel start and successful on first attempt. Both PT speed pick ups and both Accelerometer channels funtioning properly. No liquid fuel leaks observed. Unit syncronized and ramped to 8MW for NOX water injection and then for transfer from liquid to fuel gas. No leaks observed during NOX water injection. Transfer to fuel gas successful and unit ramped to base load. Gas Detector alarm occurred at 15MW. Load was lowered until gas alarm was cleared. Unit was then shut down and LOTO applied to check fuel system components and connections for leaks. On engine fuel tubes, nozzles, and manifold connections were found secure. No visual damage to engine fuel components were observed. One flange just below the deck grate at the main flexible fuel supply hose was found with three loose bolts. The gasket was removed and replaced with a new 2” 600lb flex gasket and the bolts torqued to 100 lb/ft. LOTO was removed with this second start of the day attempted on gas fuel. Light off on gas was successful however the PT vibrations were high on this “hot start” and the unit tripped and went into it’s normal programmed two stage start with the vibrations on the PT being considerably lower on the re-start. Package gas detector alarms returned and required another shutdown for further investigation. LOTO installed and package gas detectors re-calibrated with no errors found. Floor deck plate removed and the remainder of gas piping below the deck check for security with no issues identified. Three more loose fitting connections were identified on the CDP purge overhead piping which do tie into the main “on engine” gas manifold. Those connections were secured and LOTO was removed for further operational testing. Unit still with leak on detectors and tripped when trying to enter for leak check during operation. Gathered supplies from local hardware store and customer shop to install caps and blanks for fuel system static pressure check. Report completed by Matt Wilson LM1600 8 Aero Energy LM1600 Sunday April 27, 2014 Completed installation of caps and blanks. Pressurized gas fuel system with no leaks identified on fuel tubes or hoses. Pressurized CDP side of gas fuel system and identified flexible braided hose with leak. A suitable replacement was identified onsite. It is made by Swagelock and is rated to 1200 psig. Minor change to the existing piping needed to be conducted as this new hose was longer than the original hose. The new hose and piping changes were installed and secured with the existing package bracket and clamp provisions. The damaged hose and the old CDP pipe section have been stored on top of the jet engine parts lockers. The hose can be scrapped but the piping will need to be saved for re-use when the replacement hose arrives. CDP Hose Leak View of new hose and plumbing changes Section of old CDP pipe to be saved until next visit New hose with fittings prior to installation Report completed by Matt Wilson LM1600 9 Aero Energy Rated 1200 psig as Stamped by MFG, LM1600 1” tube and elbow section used from customer parts and adapted to fit to current CDP ceiling piping configuration The unit was succesfully started on gas with no further leaks or gas detector alarms for the remainder of the day. During this time, all operating perameters appear normal. Phots of the run screen are pasted on the following pages. Report completed by Matt Wilson LM1600 10 Aero Energy LM1600 Run Data Photos from HMI and Vibration Panel @ 7.3 MW on 27 April Turbine Overview Turbine Data 1 Report completed by Matt Wilson LM1600 11 Aero Energy LM1600 Turbine Data 2 Water Injection Screen Report completed by Matt Wilson LM1600 12 Aero Energy LM1600 Gas Generator Vibration Power Turbine and Generator Vibration Report completed by Matt Wilson LM1600 13 Aero Energy LM1600 Start up details Monday April 28, 2014 Customer operations identified an oil leak causing smoking on the Power Turbine during the evening of 4/27 and GE FS returned to the site on 4/28 to investigate. Customer supported package cleaning and wipe down. Oil wetting was observed on overhead piping for Power Turbine sump ventilation system. Further inspection revealed a cracked doughnut seal on the 6” sump vent section. The complete section of piping has four such seals and all were replaced as a precaution. The walls and floor areas were wiped down and a visual inspection of turbine oil connections with no other immediate leak potential identified. The unit was started and operated to base load. During that time, visible oil debris could be seen through the package observation doors and the unit was watched through these ports to attempt to find the remaining leak. During this run, a loose flange bolt was identified on the forward LPC flange. The loose bolt location was too low to the Accessory Gearbox to enter and correct safelty and in a running condition. The unit was shut down and the loose bolt corrected. More package clean up during this shut down was conducted. During this shut down, oil accumulation was identified on the right hand side of the package near the package drain. The package drain valve was found open. This valve was close for the next start under the assumption that oil was being drawn into the package and contributing to the oil mess. More package, wall and turbine compartment floor cleaning was conducted during this shut down as well. The unit was restared and observed during the next test run to base load. During this time, visible oil wetting continued to occur on the package observation windows. The engine power was reduced and the fire system isolated so that a door could be opened for a better viewpoint and observation into the remaining leaks. During this time, more oil was identified on the right side floor and was cleaned up. Rags were affixed to broom stick and oil drips were wiped from the package sealing and turbine piping as practical in this running condition. The observation windows were cleaned. The package doors were closed and the unit was ramped up to base load again. During this ramp up, a leaking fitting was observed on the right hand side of the LPT on the CSump supply line and fitting. The was monitored for about 10 minutes and the unit shut down and isolated for up close investigation and correction. The IPB illustration on the nex page shows the location of the leak. The oil line supply to the fitting was secure with no movement to the fitting. When the tube was disconnected for further inspection, the positionable elbow became loose and it was identified that while the line connection was secure it was clear that the secondary rentention nut on the positionable elbow was not. Report completed by Matt Wilson LM1600 14 Aero Energy LM1600 At low power and intial starts, the oil leak caused by the lack of security on this secondary nut was not sufficient to notice until full power operation had been reached. The unit was re-started and monitored for the remainder of the day and no further oil leaks from this location were observed. During this run, package observation windows remained clean and oil misting throughout the package had ceased. Due to the amount of oil mess in the package from the combined sump vent and fitting leak, the package ventilation louvers and ceiling were still accumulating oil while the package fans were operating and an occasional drip from the ceiling would fall on the hot engine/ PT and cause a brief smoking. The unit ran overnight and Princetion operations monitored the unit with no other need to shut down. Report completed by Matt Wilson LM1600 15 Aero Energy LM1600 Tuesday April 29, 2014 Unit continued to operate through the day and oil drips from the ceiling due to previous leaks was subsiding. Leak location remained under observation for the day as well as visual checks through observation windows for any new leaks. Package was shut down in the afternoon for a final wipe down of walls, ceiling, floors and ventilation louvres and was restarted and operated with no other issues for the remainder of the day. Wednesday April 30, 2014 Truck scheduled for tool pick up and representatives released. END Report completed by Matt Wilson LM1600 16
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